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SPE 114255
First Application of Scale Inhibitor During Hydraulic Fracturing Treatments
in Western Siberia
K. Cheremisov, SPE, D. Oussoltsev, SPE, and K.K. Butula, SPE, Schlumberger, and Albert Gaifullin, SPE,
Ildar Faizullin, SPE, and Dmitry Senchenko, GAZPROM NEFT
Copyright 2008, Society of Petroleum Engineers
This paper was prepared for presentation at the 2008 SPE International Oilfield Scale Conference held in Aberdeen, UK, 28–29 May 2008.
This paper was selected for presentation by an SPE program committee following review of information contained in an abstract submitted by the author(s). Contents of the paper have not been
reviewed by the Society of Petroleum Engineers and are subject to correction by the author(s). The material does not necessarily reflect any position of the Society of Petroleum Engineers, its
officers, or members. Electronic reproduction, distribution, or storage of any part of this paper without the written consent of the Society of Petroleum Engineers is prohibited. Permission to
reproduce in print is restricted to an abstract of not more than 300 words; illustrations may not be copied. The abstract must contain conspicuous acknowledgment of SPE copyright.
Abstract
Problems related to inorganic scale precipitation are common in oil fields across Russia. The predominantly calcium carbonate
scale rapidly precipitates from the produced water and causes reduction in reservoir permeability, restricts fluid flow in tubing
and perforation, fails electric submersible and rod pumps, and plugs surface equipment. Local industry offers a number of
inhibitors to prevent scale deposition. Although regular and planned injection of inhibitors into producing and injector wells is
the most common method of scale precipitation prevention, no successful attempt to enhance scale prevention in conjunction
with a stimulation treatment has been documented.
This paper describes the first application of a combined scale inhibitor and hydraulic fracturing treatment in Western Siberia. It
allowed the operator to place significant amount of scale inhibitor within the propped fracture and into the adjacent formation.
The case history delineates the detailed sampling and pretreatment analysis of several oil fields with high-water-cut wells. In
some of the fields, as many as 26% of the production wells experience scale-related problems. Up to 33% of electrical
submersible pumps (ESP) failures are related to inorganic scales. Further, the candidate selection process provided ground for
detailed lab testing to optimize the inhibitor type and volumes required for the first scale-inhibited hydraulic fracturing
application in the Novogodnee field.
The pilot project wells that were hydraulically fractured with the addition of scale inhibitor yielded a threefold increase in
productivity and similar initial fluid production rates. The scale-inhibited wells did though provide sustained rates over a 3month monitoring period compared to rapid decline in production on the non-inhibited wells. At the same time, the wells
treated with scale inhibitor have provided not only sustained production but also a fourfold reduction in operating cost,
confirming the success of the pilot project.
Introduction
The prerequisite condition for the formation of scale is supersaturation of the scaling minerals in the produced or injected
water. Supersaturation of a mineral occurs when the mineral concentration in brine exceeds the equilibrium concentration.
When brine is supersaturated, salts can precipitate out of solution forming scale. The degree of supersaturation affects
precipitation rates and contributes to the scale severity. Factors leading to supersaturation are:
1.
Increased mineral concentration;
2.
Changes in temperature, pressure or pH;
3.
Mixing of incompatible waters.
Carbonate scales and in minor case some sulfate scales are without exception the inorganic oilfield scales that are found in oil
wells of Western Siberia. The most common scale deposits found in operator’s oilfields is calcium carbonate scale (CaCO3).
The uniformity of the finding is obviously related to the similarity in the widely spread reservoirs in Western Siberia1-2. This is
valid for both the oil-bearing as well as the water bearing formation that is the source of the injection water that is used for the
water flooding. The technological production processes that are prevalent in the local industry should not be neglected in the
process of scale forming. The conclusion is further confirmed by thousands of samples retrieved from electrical submersible
and rod pumps, production tubing, and downhole scale sample, from surface piping samples, and also dozens of production
fluid samples from many fields that have been analyzed by the regional laboratory on scale precipitation.
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SPE 114255
In this paper data pertinent to the fields of Sutorminskoe, Muravlenkovskoe, Novogodnee and Meretoyakhinskoe oilfields will
be represented (Table 1,
Figure 1 and Figure 2) to justify the scale prevention pilot work performed on the Novogodnee field.
Based on operator’s production department, only in the first quarter 2007 more then 350 wells have shown problems related to
scale deposits.
Oilfield
Producing wells
Scale problems
%
Muravlenkovskoe
399
104
26.1
Novogodnee
47
10
21.3
Sugmutskoe
345
58
16.8
Sutorminskoe
1055
156
14.8
Vingapurovskoe
538
28
5.2
Table 1: 2007 Scale related ESP failures for various operators’ oilfields
The reasons for ESP failures have been categorized within six major
categories:
• Solids, including proppant and proppant particles, formation
material, cement particles and rust;
• Production rate decrease causing insufficient hydrostatic head
leading to EPS pump overheating and failure;
• Critical parts failure relating to installation mechanical
damage;
• Inorganic scale build up in rotor-stator area;
• Cable damage, mainly during installation or resulting from
acid treatments;
• And others – relating to unidentified causes of pump failure.
Graphically the reasons of failure are split as in figure below:
ESP failure
15%
9%
21%
Solids
Produciton Rate Decrease
Critical Parts Failure
Inorganic Scales
Other
Cable Damage
33%
9%
Figure 1: Reasons of ESP failure
13%
Figure 2: Muravlenkovskoe field scale occurrence
Even in cases where the abrupt failure of the ESP is not the prime cause of the production stop the cumulative effect of gradual
scale build-up on production can not be neglected. A simple model can be created to evaluate the gradual loss of production
rate in low scale build up environments. Figure 3 shows the production decline plot for actual and pseudosteady state
calculated data overlay for a typical well in the Muravlenkovskoe field. The modeling was done using in house analytical
software.
Figure 4 shows cumulative production plot for actual and modeling data. Based on modeling data,
because of scales related problems the well annual production is reduced for 3400 tons of oil.
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10000
8000
25
Actual data & No Scale Prevention
Model-based data
20
Oil, tons
Oil, tons/day
Cumulative production
Production decline
30
15
6000
4000
10
2000
5
40
60
80
100
120
140
160
180
200
220
240
260
280
300
320
340
360
Days
Actual data
Modeling data
0
1
20
40
60
80
100 120 140 160 180 200 220 240 260 280 300 320 340 360
Days
Figure 3: Well A - production decline, Muravlenkovskoe field
Figure 4: Well A - cumulative production
The above example does not include any downtime in production from well being shut-in, downtime caused by waiting on
workover rig or on pump replacement and the resulting deferred oil and reduced cash flow. Nor does it include losses in
productivity that may occur during the workover cycle. These direct and indirect and indeed very realistic expenses are to be
taken into account by the operator when the well is shut down because of scaling. Therefore scale deposition prevention can
provide significant positive impact on the field economics. The assessment of scaling and scale type is the first step in the
scale prevention process. The following paragraphs will deal with these steps.
Scale Characterization
It was important to qualify the scale type and the possibility of scale occurrence. Qualitative analysis of scale deposits was
performed by:
• Analysis of retrieved samples from tubing;
• Analysis of retrieved samples from failed ESP.
The tendency of scale precipitation was based on:
• Analysis of retrieved produced water samples;
• Analysis of retrieved injection water samples;
And the prediction was done either based on Stiff-Davis3-4 method or based on an internal reservoir stimulation software
program that includes a wellbore model, a reservoir model and a chemical reaction model. Based on the complete information
about the reservoir, wellbore and fluid properties the chemical model predicts the nature and extent of scaling. The model
predicts phase equilibrium using thermodynamic principles and geochemical databases. Input data such as elemental
concentration analysis, temperature, pressure and gas-phase compositions are required to predict the effect of perturbations
such as changes in temperature and pressure or mixing of incompatible waters. Samples of inorganic scale deposits collected
from tubing (Novogodnee oilfields, Meretoyakhinskoe oilfield) and broken ESP (Sugmutskoe oilfield, Muravlenkovskoe
oilfield) were showing 95% occurrence of calcium carbonate (CaCO3) (Figure 5).
Figure 5: Scale sample from retrieved tubing -well Meretoyakhinskoe-X
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Figure 6: Scale sample from retrieved ESP - well Sutorminskoe-XXXX
As a first step in evaluation of the scales samples were taken from failed ESP (Figure 6) run in different fields. A total of 19
samples were analyzed. The internal laboratory was requested to perform X-Ray diffraction (XRD) analysis to define the scale
composition. The procedure prior to any analysis consisted of cleaning of samples in xylene and methanol to remove any
remaining oil. The solvent was carefully decanted, to ensure collection of all of the particles, and the samples placed in a
drying oven until dried to a constant weight. Once cleaned the scale samples were all very similar in appearance. A typical
sample is shown in Figure 7 below:
Figure 7: Scale sample from retrieved ESP - well Sugmutskoe-XXXX
The results of the XRD analysis show that all but one of the scale samples are composed almost entirely of calcium carbonate
(CaCO3). The only exception to this is the sample collected from well in the Muravlenkovskoe field, which was found to be
largely composed of quartz (SiO2) with only a small trace of calcium carbonate. This sample was also found to include
approximately 10% metal fragments, which were removed prior to the XRD analysis.
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Table 2: Results of X-Ray diffraction analysis of retrieved samples
Scaling Prediction
Stiff-Davis method was used to predict the tendency of oilfield waters to deposit scale. The water samples from several field
have been (Table 3 and Table 4) sampled and have shown that the producing well have tendency toward calcium carbonate
deposition (Table 5 and Figure 8).
PARAMETER
pH
Bromide
Hydrocarbonate
Carbonate
Barium
Iron
Potassium
Calcium
Magnesium
Sodium
Strontium
Density at 18.50C
Sulfate
Chloride
VALUE
UNITS
8.21
3.96
493
<0.3
0.74
0.031
12
16
1.6
820
3.3
0.998
60.8
1020
-
Table 3: Formation water analysis
mg/L
mg/L HCO3
mg/L CO3
mg/L
mg/L
mg/L
mg/L
mg/L
mg/L
mg/L
g/cm3
mg/L
mg/L
PARAMETER
pH
Bromide
Hydrocarbonate
Carbonate
Barium
Iron
Potassium
Calcium
Magnesium
Sodium
Strontium
Density at 18.50C
Sulfate
Chloride
VALUE
UNITS
7.55
25.1
661
<0.3
13
3.4
39
140
13
3800
33
1.005
22.7
5980
mg/L
mg/L HCO3
mg/L CO3
mg/L
mg/L
mg/L
mg/L
mg/L
mg/L
mg/L
g/cm3
mg/L
mg/L
Table 4: Injection water analysis
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SPE 114255
Table 5: Self-scaling (% of injection water is equal to 0):
A Scaling Tendency
Muravlenkovskoe, Well 817.
100
Mg/l
80
60
CaCO3
BaSO4
40
20
0
0
10
20
30
40
50
% of Injected Water in Formation Water
Figure 8: Scaling tendency for formation and injection water mixture (from 0 to 50%):
The widely spreading scaling problem prompted the operator to search for urgent measures of remediation, prevention and
removal. The following will describe the concentrated engineering effort related to the scale prevention pilot project on the
Novogodnee field.
Case History
The work described in the paper reflects an example of a typical oilfield in Western Siberia – a brownfield that is under
aggressive production targets and the production is based mainly on ESP, where formations are hydraulic fractured to
effectively connect the lateral and vertical flow discontinuity and increase productivity. The field, like others has been placed
for many years on an intensive water injection program to maintain reservoir pressure. A high water cut is associated with the
complex flow pattern of the injection water through the reservoir. The additional uncertainty of the injection water flow is
linked to the water injection above the rock parting pressure and the thermal fracturing caused by continuous water injection.
About 4 years ago the operator started to face inorganic scale related problems. At present time both chemical and mechanical
solutions to remove scales are widely used. A lot of effort and large funds are being spent to develop scale prevention system,
including continuous dosage of scale inhibitor either on surface or downhole, periodical inhibition by scale inhibitor squeeze
treatment or inhibition of water flooding and producing wells. This is common practice in the Russian oilfields and has been
extensively documented.
Novogodnee Field
The field is located in the Western Siberian basin. The main Jurassic reservoir (JV-1) has an average permeability of 10 mD
and a net pay of 7 to 10 m. The light crude has a viscosity of 0.3 cp, a high GOR of 540 m3/m3 and a bubble point of 308 bar.
The wells are naturally flowing because of the higher reservoir pressure and high GOR, and this is more then exception after
SPE 114255
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the hydraulic fracture completion.
Producer and injector wells, drilled in the Novogodnee oilfield are typically “S”-shaped with a similar well design.
A 393 mm (15 ½”) diameter conductor hole is drilled vertically to 360 m TVD and a 324mm (12 ¾”) diameter casing is set.
The 295 mm (11 5/8”) surface hole is kicked off at about 400 m or as required for trajectory optimization with build rates at 3
to 4º/30m. The inclined section is maintained to 1500 m TVD. A 245 mm (9 5/8”) intermediate casing is run to a measured
depth of approximately 170 m. Finally, a 216mm (8 ½”) production hole is drilled till planned TD (about 3000 m TVD) and
cased with 178 mm (7”) casing at ~3300 m MD. After perforating and hydraulic fracturing the producing zone, a 89 mm (3.5”)
tubing string is run with a packer set above the reservoir.
Methodology for the pilot project
Oilfield scales can be removed by
mechanical means or by chemical treatments
using acids and other solvents. The method of
scale removal is selected based on the type of
scale formed and where it is deposited.
Mechanical methods are effective against
thick scales formed in tubulars, but cannot
access scales formed in formation or proppant
pack. Mechanical methods are often more
expensive since they require workover rigs or
coiled tubing units. Chemical treatments can
be applied but will prove only somewhat
effective in dissolution of sulfate scales and
scales deposited deep in the formation or
proppant pack. Scale build up restricts the
flow path of the formation fluids to surface,
hence production will suffer until the scales
are removed. Therefore, prevention of scale
deposition is the best strategy in dealing with
scale problems.
Scale prevention can be accomplished by
using scale inhibitors6-8. The common oilfield
scale inhibitors used by the industry are
phosphorous compounds or polymers such as
organo-phosphonates, polyacrylamide and
polyacrylate. These inhibitors minimize scale
deposition by disrupting scale nucleation
process and/or scale crystal growth and
adherence by adsorbing onto the scale species
at the active growth sites and thus blocking
their growth.
Injector rows
Area of Scale Prevention Pilot Project
Figure 9: Novogodnee Field
To effectively prevent scale formation over a long period of time, an inhibitor must have the character of being retained in
the formation or the proppant pack and released slowly. The common scale inhibitors in use are retained in the formation by
either adsorbing to the pore walls or precipitating in the pore space. As the formation water is produced, the inhibitor desorbs
or dissolves slowly into the produced water, and if the inhibitor concentration stays above a certain threshold level, it will
provide the protection against scaling. This threshold is commonly called minimum inhibitor concentration (MIC) and for a
given inhibitor can be in the range between 5 to 10 ppm.
The scale inhibition method described in this paper essentially consists of a scale inhibitor added to a conventional fracture
treatment5 thereby eliminating a separate inhibitor squeeze treatment. As the inhibitor is mixed into the fracturing fluid during
the treatment the inhibitor is well mixed and dispersed throughout the entire fracture. In addition to the benefit of this unique
scale inhibitor placement the propped fracture itself helps control scale by reducing the pressure drawdown at a given
production rate and hence the propensity for scaling resulting in longer and better productivity of the well. Although the
precipitation of the applied scale inhibitor occurs fairly quickly, an extended shut-in period is not necessary to facilitate
precipitation. However a 12 hours shut-in period was performed after the scale-fracturing treatment to ensure success on this
pilot project.
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SPE 114255
The volume of scale inhibitor used was pre-selected based on laboratory testing to provide effective protection of the well
against carbonate scale. The targeted protection time is commonly six or more months, if possible. The scale inhibitor volume
was estimated based on the predicted water production rate and assumed inhibitor return concentration for a sox month period.
To establish the duration of the scale protection method, the required volumes for forthcoming treatments and the
requirements of re-inhibition, post-treatment scale inhibitor returns monitoring is critical for the success of all scale inhibition
treatments. It requires a commitment of resources for periodic water sample collection and analysis.
Monitoring of the scale inhibitor returns in produced water was based on quantitative determination of water soluble
polyacrylates. The method requires several basic steps:
1. Suppression of ions in the aqueous system with 1N HCl acid;
2. Adsorption and concentration of the suppressed ions onto a silica-gel adsorbent;
3. Desorption of the adsorbed ions from the sorbent with eluant;
4. Formation of a red colored complex at addition of potassium thiocyanate;
5. Measurement of the transmission on the spectrophotometer at wave length of 480 nanometers. A results must be
taken as ppm from calibration graph.
To compare the effectiveness of the scale-frac treatment post frac production from three offset wells data was reviewed.
All wells were producing from Jurassic formation – JV1-1 (Figure 10). Water flooding system is used for reservoir pressure
maintenance (Figure 11). As result of water break through both wells have extremely high water cut (up to 98%). The only
method of increasing production economically is by hydraulic fracturing, which provide significant liquid production increase
whereby decreasing water cut to 90-95% (in average oil production increase is about 35 to 40 tons of oil/day/). The main
reason of scaling is mixing of incompatible formation and injection water.
Well XXX2-Y1
Treated with
scale inhibitor
Well XXX0-Y1
No scale inhibitor
Zone treated
Figure 10: Electric logs of the off-set wells treated and untreated with scale inhibitor
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Well XXX2-Y1
Treated with
scale inhibitor
Well XXX1-Y1
Treated with
scale inhibitor
Injector lines
Well XXX0-Y1
No scale inhibitor
Figure 11: Map showing the location of the offset wells
Prediction of calcium carbonate deposition was performed using scale prediction method based on determination of
solubility index using Stiff-Davis equation. Calcium carbonate precipitation is caused by a shift toward carbonate in the
carbonate-bicarbonate-carbon dioxide equilibrium. At negative equilibrium, the precipitate goes back into solution and
calcium carbonate deposit does not occur. As equilibrium is positive, the brine is supersaturated and precipitation occurs. All
of the wells show tendency toward calcium carbonate deposition
LABORATORY REPORT
Novogodnee Field, well XXX0 pad Y1
Prediction of Calcium Carbonate Deposition
Ca++
Mg++
Na+
Fe++
CATIONS
mg/L
200.00
48.84
9926.96
0.40
meq/L
9.98
4.02
431.80
0.01
Ion
Concentration mg/L
Na
9926.96
Ca
200.00
Mg
48.84
830.00
Cl
2.00
SO4
0
CO3
1220.00
HCO3
Total Ionic Strength
SI = pH - pCa - pAlk - K =
2.66
ClSO4-HCO3-
ANIONS
mg/L
830.00
2.00
1220.00
BHT degC
85
Ionic Strength
0.2184
0.0100
0.0040
0.0116
0.0000
0.0000
0.0098
0.2538
pH
7.92
meq/L
23.41
0.04
19.99
pCa
2.302
"Stiff-Davis" equation indicates that this water has a Stability Index of
A positive index indicates a tendency toward calcium carbonate deposition
pAlk
1.699
2.66
Table 6: Scale prediction analysis for well Novogodnee-XXX0
The first fracture treatment on well XXX0-Y1, Novogodnee oilfield was performed in May 2007 using water based
crosslinked borate frac fluid with a gel loading of 4.8 kg/m3. Initial post frac fluid rate was as high as 450 m3/day and an
incremental oil rate of 62 ton/day. After 13 days of production the well was shut down due to scale precipitation in tubing,
casing, perforation and proppant pack. Workover operations, including matrix acidizing and drilling, lasted 62 days. After that
the well was producing for 11 days, and was shut down for the second time due to scale build up (Figure 12). After three
workover operations the nearby injector well have been augmented with a scale inhibition injector pump after which further
scale caused shutdowns were omitted and the production stabilized at 280 m3/day and a productivity index (PI) of 2.3
m3/day/atm was calculated based on measured rate and drawdown.
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SPE 114255
Post frac Production - well XXX0-Y1, Novogodnee oilfield
6
Total liquid production, m3/day
500
5
400
4
300
3
Qliq
PI
200
2
100
0
23-May 12-Jun
1
0
2-Jul
22-Jul 11-Aug 31-Aug 20-Sep 10-Oct 30-Oct 19-Nov 9-Dec 29-Dec 18-Jan
Date
Figure 12: Post Frac production – well XXX0-Y1, Novogodnee oilfield
The most difficult parameter to take into consideration is the loss due to production decline of a producing, hydraulically
fractured wells because of scale deposits in proppant pack. The scale deposits are decreasing the permeability of formation and
proppant pack, by precipitation in pore space. This permeability decrease results in significant reduction of production. The
response of the well Novogodnee XXX0-Y1 with the increasing PI after the scale inhibition injection has started on the near
by injector wells can not uniquely explained, as it can be explained by proppant pack clean up after initial three workover
operations, or even because of the reservoir pressure increase, related to the increased number of injector put on line.
At the time of the initial occurrence of scaling problems on well XXX0-Y1, it was decided to treat the off-set wells with scale
inhibitor that is incorporated into the hydraulic fracturing treatment. Before the treatment, the same scale precipitation
prediction has been performed on the off-set wells to well XXX0-Y1. The laboratory analysis of the formation waters and the
precipitation prediction confirmed both off-set wells XXX1-Y1 and XXX2-Y1 are prone to calcite scale precipitation (Table 7
and Table 8).
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Prediction of Calcium Carbonate Deposition
Novogodnee
WELL
XXX1
PAD
ClSO4-HCO3-
mg/L
15500
10
397
Ionic Strength
0.2134
0.0280
0.0060
0.2170
0.0002
0.0000
0.0032
meq/L
437.20
0.21
6.50
Ca++
Mg++
1.86
= pH - pCa - pAlk - K =
7.4
XXX2
meq/L
600
29.94
Cl-
pAlk
Stiff-Davis" equation indicates that this water has a Stability Index of
positive index indicates a tendency toward calcium carbonate deposition
mg/L
meq/L
18000
507.71
61
5.02
SO4--
0
0.00
477.56
HCO3-
427
7.00
Fe++
0.20
0.01
Concentration mg/L
Ionic Strength
BHT degC
Na
10979
0.2415
93
Ca
600
0.0300
Mg
61
0.0050
Cl
18000
0.2520
SO4
0
0.0000
CO3
0
0.0000
427
0.0034
SI = pH - pCa - pAlk - K =
2.187
Y1
10979
Total Ionic Strength
1.855
PAD
ANIONS
mg/L
HCO3
pCa
WELL
Na+
Ion
BHT degC
93
0.4678
pH
Novogodnee
CATIONS
ANIONS
meq/L
27.94
6.03
421.93
0.01
Concentration mg/L
9700
560
73
15500
10
0
397
otal Ionic Strength
FIELD
Y1
CATIONS
mg/L
560
73
9700
0.20
Prediction of Calcium Carbonate Deposition
0.5320
pH
7.4
1.92
pCa
pAlk
1.825
2.155
"Stiff-Davis" equation indicates that this water has a Stability Index of
A positive index indicates a tendency toward calcium carbonate deposition
A negative index indicates a corrosive condition but no deposition
1.86
Table 7: Scale prediction well Novogodnee-XXX1
1.92
Table 8: Scale prediction well Novogodnee-XXX2
The hydraulic fracture treatment on well XXX1-Y1 was performed in August 2007. Scale inhibitor was added during the pad
stage and all proppant stages in concentration 15 l/m3. Post frac incremental oil rate averaged 40 tons of oil per day and total
liquid production rate averaged 450 m3/day. Figure 13 shows the post-frac liquid production rate and calculated PI for the first
five months after treatment showing no significant production decline (PI > 3.0 m3/day/atm).
Post frac Production - well XXX1-Y1 Novogodnee oilfield
10
600
Total liquid production, m3/day
9
500
8
7
400
6
5
300
Qliq
PI
4
200
3
2
100
1
0
1-Jul
0
21-Jul
10-Aug
30-Aug
19-Sep
9-Oct
29-Oct
18-Nov
8-Dec
28-Dec
17-Jan
Date
Figure 13: Post Frac production – well XXX1-Y1, Novogodnee oilfield, treated with scale inhibitor
Subsequent fracturing treatment with scale inhibitors was performed on well XXX2-Y1, Novogodnee oilfield in
August 2007. The same approach to scale inhibitor volume estimation was used for this treatment as well and the inhibitor was
added on pad stage and all proppant stages in concentration of 15 l/m3. Because of a premature screen-out only 60% of the
designed amount of scale inhibitor was placed into formation and proppant pack. Post frac incremental oil rate averaged 29
tons of oil per day and total liquid production rate averaged 420 m3/day. Figure 14 presents the liquid production rate and
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SPE 114255
calculated PI for the first five months after treatment, showing no significant production decline (PI > 4.0 m3/day/atm) that
would indicate scaling.
Post frac Production - well XXX2-Y1 Novogodnee oilfield
10
Total liquid production, m3/day
600
9
500
8
7
400
6
5
300
Qliq
PI
4
200
3
2
100
1
0
0
1-Jul
21-Jul
10-Aug
30-Aug
19-Sep
9-Oct
29-Oct
18-Nov
8-Dec
28-Dec
17-Jan
Date
Figure 14: Post Frac production – well XXX2-Y1, Novogodnee oilfield, treated with scale inhibitor
The inhibitor return monitoring process started on both wells immediately after the production commenced. In agreed
time intervals produced water samples from both well were collected, and send to the local client support laboratory. The
samples were analyzed to determine the inhibitor concentration. In practice, it was noticed that the measured inhibitor return
concentration were reduced relatively quickly to low but stable concentration levels. Figure 15 and Figure 16 show the results
of the scale inhibitors return concentration monitored for well XXX1-Y1 and XXX2-Y1, showing continuous presence of
scale inhibitors for five months after the treatment.
Inhibitor Concentration
(PPM)
Scale inhibitors m onitoring - w ell XXX1-Y1, Novogodnee oilfield
1.4
1.2
1
0.8
0.6
0.4
0.2
0
22-Aug 11-Sep
1-Oct
21-Oct
10-Nov 30-Nov 20-Dec
9-Jan
Date
Figure 15: Scale inhibitors monitoring - well XXX1-Y1, Novogodnee oilfield
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Inhibitor Concentration
(PPM)
Scale inhibitors monitoring - well XXX2-Y1, Novogodnee oilfield
24.0
22.0
20.0
18.0
16.0
14.0
12.0
10.0
8.0
6.0
4.0
2.0
0.0
9-Aug
29-Aug 18-Sep
8-Oct
28-Oct
17-Nov
7-Dec
27-Dec
16-Jan
Date
Figure 16: Scale inhibitors monitoring - well XXX2-Y1, Novogodnee oilfield
Although the MIC reached low values relatively quickly after production started, both off-set well have produced without
interruption for more then five months, reducing the operating expenditures to a quarter of the cost of the non-treated well.
Conclusions
The success of the pilot project can be defined through the following conclusions:
- Production related problems related to scale deposition in the production system were confirmed;
- The analysis of current scale deposits confirmed that in majority of the cases calcium carbonate scale is formed;
- Scale prevention technology such as combining scale inhibitor deposition in the propped fracture greatly improves the
production life of the well;
- Significant operating costs can be saved with a minimal investments and upgrade of a hydraulic fracture treatment to a
scale and fracture treatment.
Acknowledgements
The authors wish to thank Gazprom Neft and Schlumberger for the permission to publish this paper.
Nomenclature
PI
TD
MD
BHT
TVD
GOR
Qliq
MIC
= Productivity Index, m3/day/atm
= Total depth, m
= Measured depth, m
= Bottom hole temperature, °C
= True vertical depth, m
= Gas oil ratio, m3/m3
= Liquid production rate, m3/day
= Minimum Inhibitor Concentration, ppm
Subscripts
liq
= liquid
14
SPE 114255
References
1.A.I. Voloshin et al “Scaling Problems in Western Siberia”, paper SPE80407 presented at the SPE 5th International Symposium on Oilfield
Scale , Aberdeen UK, 29-30 January 2003
2.V.V. Rsgulin et al.: ’The Problem of Scaling and Ways to Solve it in the Oilfields of Rosneft Oil Co” paper SPE104354 presented at the
2006 SPE Russian Oil and Gas Technical Conference Moscow, 3-6 October 2006
3.Stiff H.A. and Davis L.E.: “A Method for Predicting the Tendency of Oil Field Water to Deposit Calcium Sulfate” paper SPE 00130
presented at the Fall Meeting of the Petroleum Branch of Oklahoma City, Okla. Oct. 3-5 1951.
4.Stiff H.A. and Davis L.E.: : “A Method for Predicting the Tendency of Oil Field Water to Deposit Calcium Carbonate” paper SPE 952213
presented at the Houston meeting, Okla. Oct. 1-3 1952.
5.Cowan T.L., Delgado E.E., Lange G.V. and Gordon J. E.: “Successful Application of a Scale Inhibitor in Borate Fracture Fluids: A Field
Study”, ”, paper SPE 59542 presented at the 2000 SPE Permian Basin Oil and Gas Recovery Conference held in Midland, TX, 21–23
March.
6.Tomson M. B., Fu G., Watson M. A. and Kan A. T..: “Mechanisms Of Mineral Scale Inhibition”, paper SPE 74656 presented at the 2002
SPE Oilfield Scale Symposium held in Aberdeen, United Kingdom, 30–31 January.
7.Powell R. J., Fischer A. R., Gdanski R.D., McCabe M.A., and Pelley S. D.: “Encapsulated Scale Inhibitor for Use in Fracturing
Treatments,” paper SPE 30700 presented at the 1995 SPE Annual Technical Conference and Exhibition, Dallas, TX, 22-25 October.
8.Maschio L., Cherian B., Lungwitz B., Tyndall M., Garcia M., Longwell J.:” Optimization of a Scale Treatment in the Uinta Basin – A
Case History”, paper SPE 107993 presented at the 2007 SPE Rocky Mountain Oil & Gas, Denver, Colorado, U.S.A., 16–18 April 2007
Conversion Factors
atm
bar
bar
°C
cp
m
m3
MPa
md
g
kgPA
tons
×
×
×
×
×
×
×
×
×
×
×
×
1.013250
1.450377
1.0
(1.8×°C)+32
1.0
3.28
6.28981
1.0
9.869
2.205
8.33
9.071847
E + 05
E + 01
E + 05
E + 03
E + 00
E + 00
E + 06
E - 16
E - 03
E - 03
E + 06
= Pa
= psi
= Pa
=°F
=Pa⋅s
=ft
=bbl
=Pa
=m2
=lbm
=PPA
=g
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